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welshlee

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Posts posted by welshlee


  1. found a untouched air box & pipe still got the snorkal & paper filter in it.sounds quiet now.

    also done the isv reroute.made the car great. 10psi at 2rpm all the way to 15psi at 5rpm.

    cant get over how the car drives now instant power from low to high rpm

    also fitted a new boost gauge with black face & smoke glass,

    goes black when engines off.

     

    [ATTACH=CONFIG]69244[/ATTACH][ATTACH=CONFIG]69245[/ATTACH][ATTACH=CONFIG]69246[/ATTACH]


  2. i fitted the isv re-route today got all bits off the net. fitted them this afternoon then went out for a rip

    and car drives a bit different and and now getting a high pitched noise

    but apart from that its pulling very well getting 15psi at 5rpm now

    the car now drive like i wanted to go.instant power all through the rev range

    3/4 rpm gives a nice hard bit of boost .nice 1 owen g60


  3. cheers for that, il have to find a way to run a pipe in to inlet pipe, i have the plastic pipes. also is that a check valve in middle of the pipe

    i was thinking in blanker plate on charger as i gote the boost delete.also how much better and boost did you get.

    il have to look out for a boost hose with pipe coming off it if i can find one.

     

    nice 1


  4. right ive been looking through the treads about a leaky isv. some people saying they have to leak boost others say remove the isv.

    and some saying re-route.also the checkvalve mod.i seem to be losing boost again. done a boost leak test all seems ok

    so i disconnected the wire plug off the isv earlier and the car does pull a lot better & stronger;

    i did adjust isv a few weeks but i could still blow through it.sounds like its leaking when connected when i put my foot down but not always.

    i used to run 15psi,cars running 10psi just at 2 rpm then stagnates at 10 /11. now 12psi with isv wires disconnected. so some advice would be helpful,

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