steveo29
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Everything posted by steveo29
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just make sure the scraper is not sharp...something plastic would be ideal
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have you got a boost gauge to confirm if there is boost there or not? maybe a slipy belt or a hose starting to leak
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id go for a low miler if they can prove it ! the rings ,bores and everything else will have more wear
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you should find it wipes off fairly easy with thinners or carb cleaner.....mine did on a 150k engine
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senders are all good i think the isv is working as it should....its holding the revs down when its conected and the engine is cold
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id go for the vw block of possible...you see the odd pg engine for sale , but theyve all done around 100k miles so your probably going to have more issues further along the road
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only slight worry on filling it is if the sealer falls out and finds it way intot hte charger ive got to admit im not a fan of a bolt stuck in a piece of pipe..looks a bit shody
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a ported head has all the interanls smoothed out so that air can enter and exhaust cant exit faster....should be good for a nice increase id imagine your looking at £400 upwards on a exchange basis...i think g werks has started to do flowed heads
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i cant remeber the pressures it was set to, the system pressure was in spec, and i ajusted the wur with a wideband connected so that when hot its was running good tbh i think the cold fuel pressure is wrong...as it wanted to rev hard with no isv until it warmed up
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with a gauge
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okay i have a KR engined golf, its always reved rather hard on start up and ive never been able to cure it( tried messing with fuel pressure, new isv,isv control,wur etc) anyway today i thought id start it with the isv red black wire undone to see if it keeps the revs down, and on start up the revs shot round to 2-3 k and wouldnt settle ....i plugged the isv in and it dropped back my question is :oops: does that sound like incorrect cold fuel presure? as the idle is 900 when warm without the isv plugged in
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chances are its down on power with a failed gasket...certainly dont go nutting it about till its fixed its worth having new valve guides and or stem seals whiles its off...if your flush and after more power then a ported/flowed head would be a godd idea £350 is a fair bit...id do it myself
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http://the-corrado.net/.archive/forum/viewtopic.php?t=38283 ive been going nuts trying to find where my noise was from
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the blanking cap is just a rubber cap that slips over the outlet on the tb
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the pipe with a bolt is what supercharged junkie suggests is causing my noise...i fitted a proper blanking cap and im having a prob with it not sounding right as mentioned in my first post i agree the bolt stuffed in a pipe looks rank....not really sure of a nice way to do it...was hoping for lots of answers as many people do this mod
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cheers i'll have a look soon strange no one else has chimed in....must only be me n you that can hear it
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cheers i'll give that a try....thanks for responding :) is yours a fairly fat pipe..the pic shows it like a thin vac tube
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16v? upper and lower manifold gaskets and its probably an idea to get the inj inserts and seals and theyre prob leaky make sure you get the right size gasket..i.e 42/50mm
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what pipe is that mate?? how long is the pipe your usung?
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feel bad for you mate, they must have used a fair bit of force to do that...it the back of the dor marked?
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i removed the c arbon canistor on my g6o...i now have a sound which is very much like a leaky vac pipe when driving off boost..it sounds like behind dash or TB area ive used proper vac caps, and now jubilee clips...ive checked over it 3 times and cannot find a dud connection :mad: just to be clear(maybe ive missed something :oops: ) the fuel tank breather is now in the airbox, one small vac line blanked off on back of TB and a bigger one blanked off on lower TB , ive fitted a 90deg elbow for the MFA line at the fron tof the manifold! is that everything? so have i missed something...or does the removal of the CC cause increased sucky/vac leak sound on off boost driving?? :roll: :roll: its driving me mad..i cant that ive done anything wrong, yet it sounds wrong
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the tb earth lead should be fixed....it will be the earth from batt-chassis-gearbox thats causin probs
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are you sure it was the brake hose?? the flat battery/solenoid thing points to a bad earth cable on the battery
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its a sod to get out ...i broke the old one up with a screwdriver ! some peopple claim if you get a close fitting drift and pack the bush with grease it will pop out when you bash the drift?? worth a try i guess or you can find a tap that threads into it with idea that you can yank it out
